So, the dust has settled, it's bank holiday weekend. I may as well write up the episode of Castle Combe and the Spring action day.
Things started out pretty well getting ready for the day.
With lots to do, I was up at 7am to do a quick wheel alignment on the car before work:
I'd found this handy calculator online, which means the strings don't have to be perfectly square to the car, which really speeds up the setup time:
And then after a quick tweak:
This method is more accurate if you use a vernier to measure distances to 0.1mm, but for a quick check and minor change that I needed, this is plenty.
With the alignment done, I drove it to work that morning, and it was feeling really good.
I'd bedded the brakes in on the way to Guildford earlier in the week, and they were feeling strong, the car was pulling straight, and generally we felt ready.
I'd also loaded on a higher boost map, feeling confident I'd solved the minor knock issues caused by oil getting into the combustion chamber.
With everything just about ready, I even found time to have it cleaned for a change!
I offered the carwash guys an extra few quid if they could get the bottoms of the doors clean, but no matter what they tried it wasn't happening. We decided between us that the matte rough finish was infact caused by hot brake dust. That'll teach me to wash it more often in future!
Still, cleaned as best as they could, it was looking good!
We finished work around 4pm, and quickly bled the brakes on the volvo:
Before heading back to mine, loading the A3 up, applying a few stickers Clive / Aaron has sorted for the action day (thanks guys) , then going to pick up some slicks for Andy, and some fuel for the day:
Quick test fit on the volvo, it was looking good!
We arrived at the unit at 6am the next morning, and to my surprise nocturnal Sam was already there in the E36!
We parked up and began strapping the volvo onto the trailer Andy had borrowed:
Whilst the A3 sat outside warming up:
We left a bit later than planned, at 06:38, but with clear roads we were due at Combe shortly after 0800:
I must admit, I had a little trailer Envy!
A quick stop at Tot Hill for fuel and breakfast, and of course a picture of 3
I quite like the slightly more subtle look, a few silver stickers, and the brighter wheels certainly lift the car in my opinion:
McMuffins consumed, and we were on the road again:
Spirits were high for the day ahead!
We arrived at Combe shortly after 8, although due to the huge popularity of the Action days, it was almost 9am before we were inside the paddock, and straight into sound testing:
With things nice and warm, the car blew 91dBa at 4500rpm. It's well under most limits, but I always keep a record of it's results, just incase things start to get louder suggesting some repacking could be done on the rear box. All good so far though. Not bad for a £240 exhaust that's now 5 years old!
I got through an early drivers briefing, and got the car into the pitlane where we were setting up. Our friend James very kindly set all the tyres to 24psi for me whilst the Mission Motorsport drivers had a quick run down of the day with Jim Cameron, Mission Motorsport CEO.
James and I headed out for a few sighting laps, to warm the car up, get some heat in the tyres, and generally check things were OK.
I did a lap on low boost, and straight out of the box things were feeling really good! the car seemed to brake and turn well, and the medium compound NS2Rs felt very good straight from cold.
After a lap I turned the switch to full boost, as that's what I intended to run all day. the car didn't feel quite as quick as I was used to, and on watching the boost guage it was clear that my actuator had relaxed a little. It was slow coming onto boost, and peak boost was a few psi lower now that things had heated up. not the end of the world, and very easily fixed by adding half a turn of preload, but worth noting all the same.
Sadly, what was more worrying, was the amount of smoke I could see in the mirror within a few corners of turning the car to high boost.
Argh. This doesn't sound good. we were at Bobbies, very close to the pitlane entrance, and it was clearly coming from the exhaust, so at this point I wasn't too worried about dropping fluids on the track.
I stuck to the extreme left hand side, and coasted all the way to the pitlane.
Back on throttle once in the pitlane to keep the car moving, and the smoke screen behind became rediculous. With a light tail wind the smoke was engulfing the whole car.
This seemed pretty serious at this point.
The Marshall was kind enough to point out to me that the car was smoking a little, and advised me that I wouldn't be allowed back on track if I had an oil leak. Thanks for that. I wasn't aware!!!
Bonnet up to investigate, and things seem became pretty clear.
Oil at the end of the air filter. Not cool!
I disconnected the catch can drain line to see if there was anything in it:
Ah.
Thanks to
@Rainbird for this fetching picture:
2 can play at the daft pictures game
Not a great start to the day.......